Green cooling, heating initiatives keep gears cool and precise
November 1, 2010
During these cold winter months, it may be hard to recall how heat can be harmful, but for precision gearmaker Forest City Gear, excess heat is an enemy to a quality product. Achieving the tight tolerances inherent in precision gearmaking requires keeping the metal at a constant temperature. Forest City Gear takes a cool green approach to cooling its facility, machinery, and employees with energy-efficient air conditioners, V-Blox power surge equipment, chiller/filtration system, high-efficiency ceiling fan, white roof, and other initiatives to chill its electricity bills.
During these cold winter months, it may be hard to recall how heat can be harmful, but for precision gearmaker Forest City Gear, Roscoe, Ill., excess heat is an enemy to a quality product. Achieving the tight tolerances inherent in precision gearmaking requires keeping the metal at a constant temperature. A heat increase of even 20 degrees will change the gears’ dimensions dramatically. Boeing, Airbus, Siemens Medical, Bradshaw Medical, Baldor Electric, Thermadyne, and Harley-Davidson depend on the accuracy of the company’s gears.
Too, the company’s state-of-the-art machines are all computerized and very sensitive to high temperatures, so keeping the facility cool is critical.
Also adverse to efficient manufacturing are the high electricity bills that can result from cooling a 30,000 square-foot facility. Escalating electricity bills were wreaking havoc on the manufacturer’s operating costs and taking a bite out of its $12 million annual sales profits.
When a monthly electricity bill climbed to $15,000, Forest City Gear President Wendy Young decided it was time to put a freeze on rising bills.
“When our electric bills started increasing about five years ago, we started looking hard at costs. Fifteen thousand was really an eye-opener for us,” Young said. “The global manufacturing atmosphere is highly competitive. From an economic perspective, we had to look at ways to keep our costs from increasing for us to remain competitive.”
The manufacturer hired an independent consulting firm to do a cost-benefit analysis and compile a list of options for lowering costs. The company initiated several of the suggestions over a five-year period, starting with those with the shortest ROI.
“We didn’t implement everything right away, but we did look at the things that had the shortest payback period and that were affordable at the time,” Young said.
Energy-efficient cooling and heating system initiatives included:
Window Coverings. Window treatments and covers were installed first and had a four-year payoff. “All of our windows have 3M window covering treatments on them to prevent heat from coming in during the summer and from going out in the winter. The window treatments were the first thing we did because they were economical and we earned our money back in four years,” Young said.
Chiller/Filtration. “Our biggest energy-saver and our most costly investment was our Oberlin oil chiller and filtration system for the gear grinding,” Young said (see Figure 1).
“We have six gear-grinding machines out here that all require their own filtration systems,” she explained. The heavy machining, gear-grinding machines are huge power consumers. The equipment generates a lot of heat too. Because most of the production equipment is very high-end, state-of-the-art CNC equipment with delicate electronics, maintaining the temperature is critical.
“Also their footprint is huge, and our space is limited, so installing the Oberlin fulfilled a couple of needs. Number one, we were able to remove these machines that were throwing off 114 degrees while they were running.”
“Now they go through the Oberlin, which is out in the back warehouse, and then the other half of the system sits outside.” As an added bonus, the chiller uses outside air for chilling the oil anytime ambient air temperature is 50°F or below.
“Number two, it opened floor space so we could buy production equipment and put it on the floor,” Young said. “Needless to say, it lowered our heat index in the building, and then the production space we gained was a huge byproduct,” she said.
The lowered facility temperatures had a third, important effect, Young said.
“Not only do the machines need the cooler air, but when our employees have to work in 90-degree heat, they’re uncomfortable, they’re sluggish, it slows them down, and they think we don’t care about them. That’s probably the most important reason. If they’re not there to run the equipment, we have nothing,” Young added.
Energy-efficient Air-conditioning Units. The company replaced its old air conditioning units with larger, more efficient units that cool more using the same amount of amperage, said Larry Cass, safety manager.
“The new AC units are larger – 25s instead of 20s – but the energy usage is the same,” Cass said. “We’ve gotten bigger, more efficient units and more cooling for the building as a result, for the same money.
“We’re seeing improvements not only in the physical facility, but also in the production equipment, because despite the relatively small size of the building, we consume a lot of power with the heavy machining equipment that we use.”
Heat Vented From Air Compressors. The air compressors have been set up to exhaust out of the building in summer and reverse the venting into the building in winter, Cass said. “So the warm exhaust helps heat up our dock area. Because we can vent the heat from the air compressors back into the warehouse, that is a big savings. It’s a big space. Maybe 2,000 or 3,000 sq. ft. back there. It’s free heat for us all winter long,” Cass said.
High-efficiency Ceiling Fan. “That big fan out there really does move the air,” Cass said. “Compared to the cost of an air conditioner, it’s a small percentage and it covers a big area.”
The manufacturer also implemented several operational energy reductions:
Air Compression Leaks Sealed. One low-cost energy conservation effort was simply tightening air compressors and hoses.
“We have air hoses all over the plant, and our compressors are in the back. We were leaking so much air constantly, you could walk into the shop and hear this hissing sound, but nobody paid attention because it was just always there,” Young said. “So we went through and sealed 99 percent of those leaks just going through the lines and tightening and sealing them.”
The company continues to check for leaks in the compressed air system annually, Cass added.
Power Protection Installed. Recently the manufacturer installed V-Blox power protection/power factor correction units. The units go in front of the power panels on the machines that draw the most power (see Figure 2).
“All the energy coming into the building comes in at different rates, so we have power surges all day long, and it’s very hard on our equipment,” Young said. “Too, we’re paying for all of that extra electricity.”
The system works twofold, Cass said. “It blocks any spikes that might happen because of lightning or from the utility company. It blocks those surges so they won’t blow a microprocessor of some kind, which has happened to us before.
“The other thing the system does is … what you get off the line typically is higher than what the motor draws. That’s just the way electricity works,” Cass continued. “This puts a block on that so we don’t use any more energy than what the motor needs. It helps the motor be more efficient, and it matches the consumption to the power usage.
“This is not only controlling the incoming power from the main to flatten that curve out a little bit, it’s also allowing all of the drive motors and the electrical power equipment on each machine tool that we run here to run at a lower speed and greater efficiency,” Cass said.
The proof is in the kilowatt-hour (kWh) reduction, Young said. “It lowered our electricity consumption on the machines by about 20 percent, and our machines run cooler and more efficiently. We spent about $80,000 on it, and we’ll see the payoff in three to four years,” Young said.
Young looked at other energy efficiencies that could be gained in the building and on the grounds.
“We changed every overhead light out in the shop from T-12 to T-8 using 25-, 28-, and 32-watt lamps,” Young said. “The lighting was expensive, but the payoff was pretty quick; about three years.
“The day after the lights were installed, people were coming in and saying ‘It’s too bright in here!’ and we said, ‘You’ll get used to it.’ And they did in about a day. It was so much nicer,” Young said.
In addition, Forest City Gear implemented a robust recycling program:
White Reflective Roofing. “We’re looking at putting a single, uninterrupted white reflective roof sheeting on the building’s roof to reflect the heat. There are no seams, so there wouldn’t be any leaks. That’s the newest thing we’re doing,” Young said.
The company is also investigating installing a solar energy system on its roof.
Forest City Gear was recognized in 2008 as a green business leader by the Winnebago County Green Business Coalition. In 2009, it received the Outstanding Corporate Friend of the Environment Award from Keep Northern Illinois Beautiful (KNIB).
But the accolades were not the reason for the sustainability efforts, Cass said. “You do it because you care about the environment, but also it makes economic sense. It’s more efficient to manufacture that way. It is cheaper to manufacture using green initiatives.”
Forest City Gear’s sustainability efforts and energy efficiency approaches have not reduced its electricity bill so much as allowed the gearmaker to add equipment and increase productivity without increasing electricity consumption.
“It’s hard for us to measure how much our electric bill has been reduced because rates keep going up and we’re buying more machines,” Cass said. “Productivity per square foot is substantially higher.”